Tonight I drilled the control stick bases. This was quite easy once I found a level surface. I found the superglue didn’t bond well to the steel, so my initial match drilling of the bolt holes was not ideal. Still, everything came out well within an acceptable margin of error.
Match drilling the bolt holes between the stick bases and the sticksLining up the stick bases and waiting for the super glue to dry
Tonight I installed the autopilot pitch servo. This was fairly easy, although it was a bit of a stretch at times to reach the back side of the servo to get bolts installed and torqued.
Thanks fully everything installed easily, and I was able to route the wiring easily, cinching down the zip ties too.
The autopilot servo, with arm removedThe autopilot pitch servo installed in the aft fuselage.
Tonight I installed the bellcrank into the fuselage, and connected the pushrods to the idler brackets. I was relieved to discover that the idler bracket still swung freely and no more sanding was needed.
Bellcrank installed and torquedIdler bracket connected to both pushrods and torqued
Tonight I assembled the bellcrank and pitch servo bracket. Everything was straightforward except the mounting of the two angles onto the bell crank plate. The alignment of the bolts took some negotiating, but after a few attempts, I was able to get it installed and torqued.
Nutplates installedBellcrank riveted Bellcrank installed and connected to the pushrod, ready for installationPushrod installed and final torqued
Tonight I final torqued the pushrod jam nuts, and then installed the first pushrod into the fuselage.
Before I final torqued the jam nuts, I made a simple measuring device to ensure I had the right dimensions on the pushrods. I installed a temporary bolt into a length of wood, and using this to pin down one end of the pushrod, measured the center of the hole at the other end. This seemed to work well, and after a few minor adjustments I torqued down the jam nuts and marked with torque seal.
Bolt holding one end of the pushrodMarking the length of the pushrod for measuringFinal torque applied to jam nuts on the rod end bearings.
Installing the first pushrod into the fuselage turned out to be harder than I imagined. It gets fed through from the bulkhead at the back of the baggage compartment, which is easy, but getting final torque on the nut was really hard due to the limited access. It took an hour just to get the one nut torqued correctly.
The troublesome bolt, final torquedFor context, the pushrod connects to the torque tube in the cockpit and extends aft to the area just behind the flap motor
Tonight I found the rest of the elevator control parts, drilled, cut, deburred and primed them all. One of the parts has an optional lightening hole, I drilled it out, but only to 1 inch diameter, as I don’t have a 1 1/4 inch step drill. I don’t think that matters, but will find out later!
I also located the elevator autopilot kit, and will install the motor at the same time as I install the rest of these parts.
Primed parts. I used some dowels to suspend the pushrods while painting. That worked well.
Tonight I finished assembling the elevator pushrods. This was a case of lightly sanding down the primer and installing the caps in the end of the tubes and riveting them together. This ended up being time consuming, but not very difficult. Once these get primed on the outside, they will be finished and ready to had the rod end bearings installed.
Messy desk, but everything I need to pop rivet these pushrodsOne end of one of the three pushrods
Tonight I started making up the elevator pushrods. There are three aluminum tubes that have caps installed, with threads for rod end bearings. I final drilled the holes in all three pushrods and primed the inside of the tubes.
The plans ship with a template, which I used to trace onto some thin trace paper. I’m glad I traced it, vs just cutting it out of the page in the plans, because I discovered the printing wasn’t to scale. The first template I made didn’t quite fit around, and when I checked the scale on the plans page I realized it was printed at about 95% true size.
Once I had adjusted for the error and made a new template I marked out the holes and drilled them using my pipe clamp.
Then with the end caps in place, I final drilled all the holes and deburred them. Then i primed the insides of the tubes and left them to dry overnight.
Pilot holes drilled in one end of one pushrodDrilling the holes. Lots of them. Clecos holding the end caps as I work around match-drilling the final size holesAnother shot of the ends being final drilled
Tonight I test fit the idler bars, and sanded down the flanges of the idler bracket to ensure clearance. These bars are responsible for the transition from one elevator pushrod to another, and must swing freely through the full range of motion. At first they were rubbing slightly on the bracket, but after some patient sanding with Emory cloth I was able to achieve the appropriate clearance. Hopefully it’s enough to still clear the bracket after I prime the parts.
The final step in the brake and rudder system is to hook up the cables to the pedals and then install the the cable guides. I counter sync the cable guides, and pop riveted them in place.
Clecos holding the rudder cable guides in place before rivetingGuides installed